Last night at about 12:00 am I had a very interesting moment while taking a friend for I ride. I was wound out in 3rd gear and let off the throttle to let the car slow down on it's own. To my surprise she did slow down.. I did not panic. I applied the brakes but at that speed and with the engine making power. This was not a quick solution. I pushed it the clutch and the motor hit the rev limiter.. I shut of the ignition and coasted about a 1/4 mile to a gas station.
I quickly jumped out and popped the rear deck lid. After a quick inspect of the Throttle Body ( TB ) it was stuck about 1/3 open. I could open it fully but when released it would not return to the normal resting position.
I cycled the TB about 10 times and when released it snapped back but felt weird like it was hitting something soft. After a few more cycles it closed and felt normal. At that time of night and with no tools it was not the best place to start tearing her apart. We started her up and eased her back to the shop.
Today I started to take it her apart. Really curious to what had happed and why Throttle plate freed up again. In the back of my mind I was thinking if I didn't find anything obvious I was going to live in fear that this could happen again anytime which is not a comforting thought.
I first pulled the bellows section out to look directly in the TB and inspect the butterflies. They looked normal and operated smoothly. I than looked inside the bellows section. I have an Accufab stiffener. When the TB was stuck open I was thinking maybe the Accufab stiffener had shifted or part of it broke off and lodged in the TB opening ?? It was fine .. At this point I was not happy about not finding anything obviously wrong.
I than looked into the outlet tube of the air box. With the bellows off you can see the back side of the air filters. Well , well I found a very obvious and unexpected problem. The filters were pushed down in the housing and un seated from the sealing channel. There were two large chunks of the seal laying on top / back side of the filter..
These two chunks were off the long side of the filter. The total length of the long side is about 8 " These two pieces added up to be about 4". I just watched Sherlock Holmes and I quickly concluded that the soft blockage I felt was,,, yes you guessed it was part of the air filter seal stuck in the TB.
I dissembled the air box to look a the air filters and see of some of the seal and fallen to the bottom of the air box. sad to say there was no pieces there so you guessed it... the missing 4" of the air filter seal was sucked into Super Charger and shredded to bits.. And you know where the remains would be resting.. Yes you are correct. They were nicely collected under the Super Charger on top of the Inter cooler.
I vacuumed out all of the large bits and sent a considerable amount of time getting the fine bits out of the small finned openings of the inter cooler.
Tomorrow I'll do some more cleaning and service the SC fluid while she's off.
I'm not sure what to say but I can give you these facts. The rubber seals on these filters was brittle and degraded upon inspection . They both were brittle and cracked. I just installed these new Ford Motor Craft filters before the rally so they have only seen about 500 miles of use.
They fit fine in the housing. The seals were soft and formable upon installation. The housing halves went back together smoothly. I have performed several air filters changes before so I am ruling out any installation issues ??
Maybe it was a bad batch of rubber or not cured properly. I have done a search and have never heard of this problem. I am not trying to cause panic . I just want you to be aware that a stuck throttle could happen to anyone at any moment . Hopefully this is an isolated case. It's a PIA to take apart the SC and clean the IC but I am very thankful nothing else bad happened to the vehicle !!
Bill or Kendal any thoughts on why the filters were pushed down? The natural suction should have drawn them Up not Down ??
I quickly jumped out and popped the rear deck lid. After a quick inspect of the Throttle Body ( TB ) it was stuck about 1/3 open. I could open it fully but when released it would not return to the normal resting position.
I cycled the TB about 10 times and when released it snapped back but felt weird like it was hitting something soft. After a few more cycles it closed and felt normal. At that time of night and with no tools it was not the best place to start tearing her apart. We started her up and eased her back to the shop.
Today I started to take it her apart. Really curious to what had happed and why Throttle plate freed up again. In the back of my mind I was thinking if I didn't find anything obvious I was going to live in fear that this could happen again anytime which is not a comforting thought.
I first pulled the bellows section out to look directly in the TB and inspect the butterflies. They looked normal and operated smoothly. I than looked inside the bellows section. I have an Accufab stiffener. When the TB was stuck open I was thinking maybe the Accufab stiffener had shifted or part of it broke off and lodged in the TB opening ?? It was fine .. At this point I was not happy about not finding anything obviously wrong.
I than looked into the outlet tube of the air box. With the bellows off you can see the back side of the air filters. Well , well I found a very obvious and unexpected problem. The filters were pushed down in the housing and un seated from the sealing channel. There were two large chunks of the seal laying on top / back side of the filter..
These two chunks were off the long side of the filter. The total length of the long side is about 8 " These two pieces added up to be about 4". I just watched Sherlock Holmes and I quickly concluded that the soft blockage I felt was,,, yes you guessed it was part of the air filter seal stuck in the TB.
I dissembled the air box to look a the air filters and see of some of the seal and fallen to the bottom of the air box. sad to say there was no pieces there so you guessed it... the missing 4" of the air filter seal was sucked into Super Charger and shredded to bits.. And you know where the remains would be resting.. Yes you are correct. They were nicely collected under the Super Charger on top of the Inter cooler.
I vacuumed out all of the large bits and sent a considerable amount of time getting the fine bits out of the small finned openings of the inter cooler.
Tomorrow I'll do some more cleaning and service the SC fluid while she's off.
I'm not sure what to say but I can give you these facts. The rubber seals on these filters was brittle and degraded upon inspection . They both were brittle and cracked. I just installed these new Ford Motor Craft filters before the rally so they have only seen about 500 miles of use.
They fit fine in the housing. The seals were soft and formable upon installation. The housing halves went back together smoothly. I have performed several air filters changes before so I am ruling out any installation issues ??
Maybe it was a bad batch of rubber or not cured properly. I have done a search and have never heard of this problem. I am not trying to cause panic . I just want you to be aware that a stuck throttle could happen to anyone at any moment . Hopefully this is an isolated case. It's a PIA to take apart the SC and clean the IC but I am very thankful nothing else bad happened to the vehicle !!
Bill or Kendal any thoughts on why the filters were pushed down? The natural suction should have drawn them Up not Down ??
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